Name | |
Spud date | 2017-10-03 |
Abandon date | |
Borehole orientation | Directional |
Measured depth | 2303.000 |
True vertical depth | 2301.150 |
Tperf | 2131.000 |
Bperf | 2259.000 |
Water geochem | |
No well data | |
Glog unavailable | |
Notes |
Service company | Halliburton |
Tool | Array Compensated True Resistivity Spectral Density Dual Spaced Neutron |
Date | 2017-10-06 |
Run number | 1 |
Driller depth | 2303.000 |
Logger depth | 2308.000 |
Log bottom | 2296.000 |
Log top | 900.000 |
Casing size | 13.375 |
Bit size | 12.250 |
Mud type | Brine |
Mud density | 8.70 |
Mud visc (plastic) | |
Mud visc (funnel) | 47.00 |
Mud ph | 8.30 |
Mud fluid loss | 7.40 |
Sample source | Active Pit |
Circulation stopped time | |
Logger on bottom time | 20:15:00 |
Time since circulation | 4.750 |
Operating rig time | |
Notes |
45229 | 2018-08-07 10:33 | dakota | CLOSED, UNHANDED |
45229 | 2018-08-07 10:33 | dakota | EDITED RUN 1 (Oct. 6, 2017) |
45229 | 2018-08-07 10:27 | dakota | EDITED WELL METADATA |
45229 | 2018-08-07 10:21 | dakota | TAKEN |
45229 | 2018-06-29 11:04 | e.haugen | TASK CREATED |
39606 | 2018-05-20 16:07 | sgainer | CLOSED, UNHANDED |
39606 | 2018-05-20 16:06 | sgainer | EDITED RUN 1 (Oct. 6, 2017) |
39606 | 2018-05-20 16:06 | sgainer | ADDED RUN 1 (Oct. 6, 2017) |
39606 | 2018-05-20 16:04 | sgainer | EDITED WELL METADATA |
39606 | 2018-05-20 15:59 | sgainer | TAKEN |
39606 | 2018-04-13 12:12 | e.haugen | TASK CREATED |
Well 05322485