Name | |
Spud date | 1944-11-28 |
Abandon date | 1992-06-05 |
Borehole orientation | Directional |
Measured depth | 3469.000 |
True vertical depth | 3463.000 |
Tperf | 2610.000 |
Bperf | 3463.000 |
Water geochem | |
No well data | |
Glog unavailable | |
Notes |
Service company | Halliburton | Halliburton | Schlumberger |
Tool | ELECTRIC WELL LOG | ELECTRIC WELL LOG | Induction Log |
Date | 1944-12-04 | 1944-12-14 | 1966-06-28 |
Run number | ONE | TWO | ONE |
Driller depth | 2670.000 | 3038.000 | 3458.000 |
Logger depth | 3459.000 | ||
Log bottom | 2670.000 | 3040.000 | 3459.000 |
Log top | 208.000 | 2670.000 | 2533.000 |
Casing size | 7.000 | ||
Bit size | 10.625 | 6.125 | 6.250 |
Mud type | OIL BASE | ||
Mud density | 83.00 | 78.00 | 61.00 |
Mud visc (plastic) | 32.00 | 35.00 | 120.00 |
Mud visc (funnel) | |||
Mud ph | |||
Mud fluid loss | |||
Sample source | |||
Circulation stopped time | |||
Logger on bottom time | |||
Time since circulation | |||
Operating rig time | |||
Notes | Mud Density in lbs per cu ft. Mentions impedence in ohms; not sure if Rm. | Mud Density in lbs per cu ft. Mentions impedence in ohms; not sure if Rm. |
86065 | 2019-07-06 08:25 | NickWaring | CLOSED, UNHANDED |
86065 | 2019-07-06 08:24 | NickWaring | ADDED RUN ONE (June 28, 1966) |
86065 | 2019-07-06 08:21 | NickWaring | EDITED RUN TWO (Dec. 14, 1944) |
86065 | 2019-07-06 08:21 | NickWaring | EDITED RUN TWO (Dec. 14, 1944) |
86065 | 2019-07-06 08:13 | NickWaring | EDITED RUN ONE (Dec. 4, 1944) |
86065 | 2019-07-06 08:13 | NickWaring | ADDED RUN TWO (Dec. 14, 1944) |
86065 | 2019-07-06 08:12 | NickWaring | ADDED RUN ONE (Dec. 4, 1944) |
86065 | 2019-07-06 07:56 | NickWaring | EDITED WELL METADATA |
86065 | 2019-07-05 16:00 | NickWaring | TAKEN |
86065 | 2019-06-19 12:38 | tsowers | TASK CREATED |
Well 03700916